Earlier this summer I was flying from Thorn Bay to Craig on Prince of Whales Island and saw what was left of a DC-3 wrecked on a salt marsh. I asked about it then looked it up on the web. here are the pictures I took and the accident report.
Terse were some lucky guys. There are mountians all arround this site.
Big Salt DC-3 Crash
report
EC-47 42-24304
EC-47 Crash Landing in Alaska, enroute to SEA (note: It was
enroute FROM SEA to Elmendorf )
From USAF Accident/Incident Report Dated 9 Nov. 68
Summary
Upon arrival at McClellan Air Force Base, California, Lt.
Colonel Ronald A. Bena, Major Jerry E. Marshall, Major Floyd J. Brazile ans
SSgt Thomas Kaminski, were directed to ferry EC-47Q #42-24304 to Southeast
Asia.
The personnel performed the following duties on the flight:
Aircraft Commander, Lt. Colonel Bena; Copilot, Major Marshall; Navigator, Major
Brazile; Flight Engineer, SSgt Kaminski. The crew departed McClellan AFB,
California, for McChord AFB, Washington, at 1930Z 24 October 1968. Flight time
enroute was four hours.
At 1500Z, 25 October 1968, the crew departed McChord AFB,
Washington for Elmendorf AFB, Alaska. Flight altitude was 10,000 feet IFR and
estimated time enroute was eight hours and thirty-seven minutes.
At approximately 1955Z the aircraft yawed to the right. Lt.
Col. Bena, the aircraft commander, feathered the right engine. The nearest
suitable landing field was determined to be Annette Island Coast Guard Station,
Alaska and an immediate turn was made toward Annette.
Altitude could not be maintained on one engine so an enroute
descent was made to 6,500 feet. The flight continued until at approximately
2020Z when the left engine lost power. The aircraft was still approximately 70
miles north west of Annette Coast Guard Air Station. Attempts were made to
restart the left engine. When attempts to restart the left engine proved
fruitless, the right engine was unfeathered and attempts were made to restart
it all to no avail.
During the descent following loss of power on the left
engine the C-47 became IFR at 5,000'. Upon reaching 3,500' a break in the
clouds to the right of the plane revealed water below. A turn was made toward
the break in the clouds and decision was made to ditch rather than bailing out
over very mountainous and wooded terrain. VFR conditions were attained at
approximately 3,000 feet. The cargo door was jettisioned in preparation for
ditching.
As a pattern was set up for a water landing, a small marsh
on the edge of the edge of a lake was observed. This lake was Big Salt Lake, actually
an inlet of salt water on the western side of Prince of Wales Island. A left
hand pattern was initiated for a gear up landing on the marsh. Final approach
was at 90 knots and half flaps. Initial contact was made almost simltaneously
by both wings on three large stumps.
The right wing was partially seperated near station 100 and
both wing tips were torn off near station 340. Ground contact was made shortly
thereafter by the rear portion of the fuselage. The aircraft traveled
approximately 430 feet after contact was made with the stumps. Initial landing
slide fairly smooth. At approximately 60 feet from the final resting place, the
right wing separated completely from the aircraft at station 100. Approximately
40 feet from the final resting place the aircraft hit another stump which
caused the aircraft to swerve to the right. Final restingplace of the aircraft
was on a salt marsh on the north side of the eastern tip of Big Salt Lake.
No serious injuries were received by the crew and the
aircraft did not catch fire. Parachutes were deployed to assist other aircraft
in locating the crash site. This was of prime significance because the aircraft
was painted with camouflage paint.
A USAF KC-135 arrived over the site approximately 30 minutes
after the crash. Contact with rescue aircraft was complicated by apparent
survival radio malfunctions. Shortly after the KC-135 arrived overhead, an
Alaskan Airline Golden Nugget Grumman Goose aircraft, an amphibian, landed on
the lake and evacuated the copilot, Major Marshall and the flight engineer,
SSgt Kaminski. The Pilot, Lt Colonel Bena and the navigator, Major Brazile
remained behind to guard the classified equipment aboard the aircraft. The
pilot and navigator were evacuated by a Coast Guard H-52 helicopter about 5 1/2
hours after the crash. Security of the aircraft was maintained by tow Coast
Guard security personnel who were aboard the helicopter which evacuated Lt
Colonel Bena and Major Brazile.
{{ NOTE: }} For those of you not familiar with the phrase,
"station 100" or "station 340" etc., these are references
in inches measured from a particular point on the aircraft. I can't recall
where the wing measurments begin, but just for the sake of clearification, we
will call it at the center of the fuselage and measuring from there outboard on
each wing. The same measuring system is used throughout the aircraft and I
believe the fuselage measurements begin at the nose and count toward the tail.
Among other things, these "station locations" are used for referances
as you see here and for weight and balance of the aircraft when loading cargo
or when making modifications that either add or deduct weight from the aircraft
structure. Hope this helps you to understand.
{{ NOTE: }}This aircraft was enroute to Pleiku according to the
report.
Having crewed and flown many hours on the C-47, this is my
opinion based primarily on the times given in the above report and the fuel
capacities and consumption of the aircraft. Having myself flown one of the
EC-47s from Grenier Field New Hampshire to Tan Son Nhut along the same route in
September 1966, I remember the 'spagetti mix' of plumbing and valves in the 2
auxilary 250 gallon fuel tanks, giving approximately 5 additional hours flying
time, it looked like a nightmare.
I have never located a report of what may have caused this
aircraft to go down, but as stated in the above paragraph, I do have an
opinion. I will, until proven wrong, believe the auxilary fuel system was the
cause. My opinion is based on normal used fuel consumption figures of 100
gallons per hour, and assuming the auxilary fuel was burned off before
switching as we did, to the normal aircraft fuel system. The aircraft had been
airborne 4 hours and 55 minutes when the right engine was lost, one of the 250
gallon tanks is now empty. At 5 hours plus 20 minutes, 25 minutes later the
left engine was lost, the other 250 gallon tank is now empty. The aircraft went
down with a normal full load of fuel, 804 gallons still in the wing tanks.
I believe that the right engine was lost after switching the
fuel supply. It is possible that in the spagetti of fuel lines and valves that
the lines or the valves were improperly installed and instead of switching to a
new fuel supply, it switched to a vent or other line with no fuel available. It
is also possible that the valves were mis-labeled. And lastly, it could have
been human error in the switching which I would first discount. 25 minutes
after the right engine was lost, the left engine is lost, and again the fuel
available and fuel consumption fall well with the range of fuel exhaustion.
This is in no way intended to place fault on the aircrew,
but is an honest oppinion of the cause of the loss of this aircraft.
James C. Wheeler MSgt Ret. Flight Mechanic - 361st TEWS Nha
Trang - 1966/67
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